I thought about just switching it off but the incentive to get another run got the better of me and i decided to go for it. It left ok but was headed slightly left so i rolled the throttle a bit and at 3.4 seconds into the run it made some unusual noises, followed by some destructive noises, a complete lack of power and then a bang followed my the death drone.
Back in the pits it didn't look good, there were chunks of casing missing, and the number 3 cyl spark plug was difficult to remove and the electrode was bent completely over. Shining a torch down the plug hole i could quite clearly see the crank. Not good!It looks like the little end of the rod has given up. There was no sign at all of a piston, pin or rings, just a smashed up barrel, and a bent and broken rod. The 4 valves of that cylinder looked pretty messed up too.
That was the end of racing for us then, but we did at least remain number 1 qualifier and will come away still with the points lead as once again no racing took place on the final day due to the weather.
the question now will be can we cobble together another engine or make repairs in time for the next round in just 6 weeks time.
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